HW 4.12 with FW 3.27 seems to have some troubles in BLDC mode, but not in FOC mode, and not with FW 2.18!
Test done with TMOTOR U8 not loaded.
BLDC mode sensored (I've glued sensors an tested with other controllers), and detection works well quickly.
Duty cycle mode works, Current mode works, but not speed mode (violent cogging, erratic, and sometime reverse rotation).
Any other people having experiment that problem?!
Have a Nice Day.
Thierry
There are known issues with BLDC hall sensors. http://vesc-project.com/node/110
Workaround is to use FOC.
Thierry
I just experienced the same cases as you. And i just want to know why?
Someone told me to changed the PID parameter, but i don't see good result.
I am wating for vedder's next code release.
Speed mode requires closed loop PID tuning, have you tuned your system?
progress report
Today i tried the foc sensorless mode, all the parameters are the same as before, but now the closed-loop pid speed control is good.
I think it is the temperature effect, because i remembered last time the motor is hot, but i'm not sure.
Anyone else has the same experience as me?
No temp problem for me.
Have a Nice Day.
Thierry