trying to run a Gimbal motor (Emax GB4008, https://emaxmodel.com/products/emax-gb4008-brushless-gimbal-motor-hollow...) on a VESC 4.12, FW 5.2, using a 3S LiPo.
"Setup Motors FOC" runs successfully, spinning the motor quite smoothly during detection. The motor direction test during detection already shows very unstable and stuttering motor run. Same for all other possibilities to spin the motor using the detected values. BLDC detection fails consistently ("Bad detection result received"). Altering the values used for detection did not help.
Any idea what I can do? :-(
Thanks and best regards